Wednesday dawned with me going to the shed and running the complete narrow gauge timetable. This is 12 trains that ply the rails from Acacia
Ridge Yard through Clapham Yard and sometimes reach Fisherman Islands
Yard. So my fleet of 4 locos and 17 wagons is not enough to run the
timetable. I actually need another loco and at least 4 grain wagons and
then the first phase of my narrow gauge loco and rollingstock fleet will be
complete. The second phase of rollingstock expansion will include adding more coal and grain
wagons, maybe 4 or 8 more of each along with a few different wagons.
I had an issue with the new dual gauge/standard gauge point
for entry into Rocklea Sidings. While all the standard gauge trains were
working, the narrow gauge trains were not travelling through the point on the
mainline. I needed to add some isolation joiners around the point, and
then feed the frog from a Peco switch connected to the point motor working this
point. I found a Peco switch lying around on the layout and soldered it
up. I jerry-rigged the dual gauge point, so that the narrow gauge track
and the standard gauge frog all worked from this switch. Testing revealed
that the standard gauge track in both directions was again working, as was the
narrow gauge traffic on the main line. However, but putting the switch
atop the point motor, the point no longer throws to the curve position (to
access the sidings) each time I push the button. However, it does restore
to the mainline correctly.
I think in the longer term, I need to acquire two auto DCC
switching frog juicers (or a similar brand) piece of kit. One will be
deployed to the point at Rocklea Sidings, and another at the Fisherman Islands
dual gauge point at the farthest end of the Yard.
So while running the narrow gauge rollingstock, I adjusted
the coupling heights on a number of narrow gauge wagons to more correctly match the height
gauge I have. These adjustments made the trains run better, as it stopped
some uncoupling events from occurring. At the end of t\he day I still had another 4 trains to run to
complete the timetable, which is what I did on Thursday.
On Friday night, I ran my track cleaning train from Grafton
all the way to Murwillumbah. On the way to Murwillumbah, I took the
mainline, and on the way back to Cassino I took the loops where I could (when there were no
trains in the way). When back at Cassino, I then went north up the
mainline all the way to South Brisbane Interstate, again taking the mainline
all the way. While at South Brisbane, I ran through the first 6 tracks at
that location . The other tracks have wagons stabled in them. The track cleaning train then ran all the way back to Dutton Park, before taking a
small detour back down the branch to Fisherman Islands. From there the
train returned all the way to Grafton. While on the way, back, I ran
through all the Loops. It was this movement that caused me to noticed the
track at Cassino Meatworks had a dead section, as did the northern end of
Cassino Yard. Another issue that developed, is that the point at Dutton
Park, which directs trains to either Fisherman Islands branch or South Brisbane
Interstate decided to not throw towards Fisherman Islands. At least I
could climb up the back of the layout and manually change that set of points if
I needed to. The set of points on the southern entry into Clapham Yard
standard gauge track 3 would also not throw, so that was added to the "to be fixed" list for after the session. So I could feel a big whoops occurring on
Saturday!
Then on Saturday morning, I had previously forgotten to move
4 of the narrow gauge trains back into place to align the narrow gauge trains with the timetable start
time. So I went down and did this. However, I was having
issues. I could not get trains to travel over my dual gauge point at
Rocklea Sidings. My Operations Session was not going to go well.
Saturday started off with the standard BBQ snags on a piece
of bread, with onions, sauce and cheese. Total crew was 11
attendees including me. Of course drinks were available of various persuasions to keep
the attendees cool. I had a few new runners this time. These guys
got a quick overview before the crew took their places. The aircon was turned on. Everyone was
handed a lanyard to attach their timetable cards to, and to provide a solid
backing if they needed to write any notes onto the timetable card, so I can go
through and correlate the issues and fix these following the session. Greg started the Raspberry
Pi for me and set the fast clock. But I told him the incorrect time – Oh
silly me! He soon fixed this, and then Arthur assumed the position of
North Coast Control. The headsets were handed out and initially what
seemed like dis-organised chaos, soon turned into a generally organised bedlam
before settling down to a more sedate operating session. We were able to
get around all the issues of dead track. Another dead track section
popped up and this is over the Richmond River bridge just south of
Cassino. This regularly occurs.
There were a number of wagon issues. One coupler jaw
snapped on a stock train. That wagon was placed in the back platform road
at Cassino. A low coupler was identified on a shunt train from Grafton to
Murwillumbah and return. A couple of trains were positioned wrongly at
the start of the session and this caused some issues with trains not being able
to exit staging due to something in front of them. But we can move trains
around to fix this and we did.
During the session, we had a few cases where shorts were
detected. We all knew who was causing them. Don’t we? Shelton
could not remember that the last 4 digits of a loco was its address. So
while trying to address 44238, accidentally sent 4423 and its ballast train
that was sitting in Fisherman Islands Yard careering into Loco Pilly. I
think he was trying to replicate the BHP run away in the Pilbara region from a
couple of months ago. A couple of other issues occurred, and we all
thought they were caused by Shelton. Upon further investigations, sure
enough most were. No one was killed, although an oil train ran into a car
at a level crossing just outside the Rocla Sleeper Siding. This has
happened before. The car sits on the road overbridge and the layout must
have been bumped and the car ran to the railway track. This shot featured
on a couple of Facebook posts by session attendees. Those running the layout via the JMRI wifi
connection through my Raspberry Pi mostly ran out of power in their phones
before the session was due to end. So there was less and less trains
running as we headed towards afternoon tea. That is why I prefer to use
the NCE Procab-R throttles, as the power lasts for about 12 months of
use. That includes all the times I fire up the layout and test it each
weekend.
I think everyone had fun. I wore the brunt of most of
the jokes, as did Shelton. But all was in jest. I think close to 40
trains were run. The timetable still has another 30 trains to complete
its cycle.
After the Operations Session, I think I found 5 cans of drink that PK squirrelled away around the layout, and today I got stuck into the "to do list". I fixed the three sections of dead track, Cassino Meatworks, Cassino Yard and the bridge over the Richmond River south of Cassino. I fixed the stock wagon with broken couplers, I adjusted the low coupler height on the MRC wagon. I decided to attend to an issue I have had at Cassino Yard for quite some time. The powered points at this location, were addressed as 1, 2, something unknown and 4. They should have been 1, 2, 3, and 4 initially and then set to 424, 423, 422 and 421 respectively. Well this has now been fixed. I did discover that there is another set of point somewhere on the layout set to 4. I'm not sure where, as it was at the other end of the layout that I could hear it throwing when I was working on Cassino Yard. I will check this out tomorrow. I ran one train twice yesterday. So I had to "unrun" it today. So I ran it in reverse to put it back. I moved another two trains that were in the wrong locations at Grafton Yard to their correct locations. More issues will be ticked off the to do list tomorrow.
Have a happy New Year everyone.
Some of the crew getting directions.
The Brisbane Limited at Acacia Ridge. On the right of this is the dual gauge, then two narrow gauge loops.
Yours truly up doing something at Rocklea Sidings.
Darryl going to do something to Chris maybe. Or was it Shelton?
Glenapp Loop. The troublesome 44238 or was that 4423 or maybe 4238?
The car ran off the bridge into the oil train.
The boys in blue out to protect the public.
Roadworks here with an ambulance coming through.
All these photos have been provided by Shelton. Thanks Mate.